Tuesday, March 19, 2013

Lee Stocking Island to Georgetown, Bahamas

This morning, we watched as all the boats left the anchorage.  We dinghied to shore and hiked over the hill to the other side of the island.  The waters looked surprising calm.  Were these the same seas we’d sailed in yesterday?  We decided to pull anchor and head out.  We were bound for Georgetown but if things got rough again, would duck in at Rat Cay (about midpoint). 

As I sailed out the cut, it was hard to believe it was the same place we’d entered yesterday.  Again, it was wind against current but there was just a gentle swell coming in from the ocean.  We’d raised the mainsail and exited the cut with such ease!  Once out in the open water, we raised the headsail and had a very nice sail south.  The waters had a slight “chop” to them but they were a hundred times better than only 24 hours ago.  It made me realize when we get to doing these longer passages, how dramatically the seas can change so quickly.  I will have to keep this in mind when we’re struggling thru rough waters that in a very short time, the seas could calm and we’ll be a peace.  But I also have to remember the opposite can occur and not get too complaisant.

About 1 hour out of the entrance to our destination (George Town area), Larry started the motor.  Our speed had dropped quite a bit and we didn’t want to enter the cut after dark.  He motored along for a brief time when all of a sudden there was a screeching siren.  We quickly realized it was the alarm for the motor.  The motor was overheated!  We shut it down (luckily we were still sailing so could still make progress) and Larry searched for the problem.  My husband is amazing.  For so many people, this would be the end and they would simply radio for help.  Not Larry.  He worked until he found the problem.  Something had been sucked into our water intake (that cools the engine) and water wasn’t flowing.  He took apart the necessary things, found a hose that would fit and was able to release whatever was blocking the intake by blowing into the hose.  (Larry:  basically, I blew air out the bottom of the boat where water normally is sucked in for the engine; blowing away whatever plastic bag, or sea life had gotten sucked in).  We started the engine again and all seemed fine.  We monitored it closely as we entered George Town but Larry’s repair seemed to work.  No more problems.

No comments:

Post a Comment